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Introduction: Harpoon Seabring

Ahoy there!

My name is Harpoon Seabring and, with a name like that, I was bound to end up in a role like this. I just graduated from Florida Institute of Technology with a BS in Ocean Engineering. While at Florida Tech, I worked in a lab that studied biofouling, with a focus on the application of ultraviolet-C light to prevent fouling growth. I was also given the opportunity to spend a few days aboard Florida Institute of Oceanography’s R/V W.T. Hogarth to test an ROV designed by myself and my senior design group. Despite being rained on every day, despite being caught in one of the first tropical storms of the hurricane season, and despite getting very seasick after one night of particularly high waves, I had an amazing time and wanted to go back out to sea as soon as possible.

Even in my free time, I spent as much time on the water as I could. Florida Tech’s sailing team took up most of my free time, and I served as the Vice President for my final year of schooling. I live in Virginia now and, at the present moment, it’s still a bit too cold to go sailing (at least with my total lack of cold weather gear). My free time is occupied by rock climbing and cycling instead. 

I look forward to working with BIOS. My time working in a lab has no doubt left me with a skillset relevant to this internship, and I hope to be a useful member of the team. Likewise, I look forward to learning about the research performed onboard and about the instrumentation the Atlantic Explorer comes equipped with. I plan on pursuing a career on marine vessels, and I believe this experience will be one big step towards that end.

 

Week 3: Ship tasks, cruises, and Maintenance Docked

April 17, 2023

Since we got back to shore we’re back to an 8-5 schedule. 

Today we didn’t have too many things to do. Oban and I were tasked with replacing one of the VHF antennas on the bridge which sounds easy, but was much more time consuming than we thought it would be. We only had to remove the old antenna and wire, and install the new one, but this took all day. Things just kept going wrong (of course). Taking down and installing the antenna was the easy part, it was the removing and reinstalling the new wire that was difficult and we’re still not done. This was mostly because it required feeding the wire through tight spaces and tubes and running it through ceiling panels which was cramped, and stuffy and took a lot of patience. We even had to drill a new hole in the ceiling so we could remove the old wire. The pictures below show the antenna we removed and the little “upside-down” U shaped wire tunnel we had to feed it through. 

April 18, 2023

Today was an important day where we tested all of the winches to make sure they can handle the weights that will be used for the next cruise, and just to make sure all is working well. Doing these weight tests also works as a calibration for the readout of the tension load on the winches. This works by using a transducer to relate voltage or current running through the wire to the force that is being ‘applied’. Essentially, the winch lifts a known weight of both small and large loads to create a linear relationship with the voltage, which is updated to the winch operating system for calibration. Below you can see some of the weights we used- which were 2,500 lb TRAIN WHEELS! So cool! We then loaded them on board the ship with the crane. 

There are a lot of winches on board the ship, and they take quite a bit of time getting used to all the names, their operation procedure (more how to handle what the winches will be used on), capacities, and maintenance. I’m still getting a hang of all the names but this is what I have come to learn so far:

DUSH 5: This is the winch that we use most often because it is used to deploy the CTD. It has an approximate load capacity/ application force of around 20,000 pounds (I think) but we have a safety margin of 5,000 pounds, which I believe is because of the capacity of the wire. The CTD weighs between 1,100 pounds and 1,600 pounds when it’s full with water. The low test for the winch was around 420 pounds and the higher test was around 4,600 pounds. The winch could handle this load just fine (which *spoiler* won’t be the case for the DUSH 4 even though it’s supposed to), however the A frame seems to be significantly strained- that’s a problem for another time. 

DUSH 4: The DUSH 4 is a hydraulic winch on the port side of the first deck. This had been strength tested to 4,600 lbs less than 6 months ago, however this time it could only lift approximately 3,400 lbs- this is not up to criteria. Lydia suggested they close some valves, and after that was done it lifted 4,100 lbs- which was better but still not what she expected.

COM7: We tested this first and began with the 460 lb weight, and then maxed it out at 2,500 lbs. This was the easiest and also the most successful.

Big Squid: This was tested with the full weights of 460 lbs and the full 4,600 lbs. 

Once all the testing was done it was about 1500- break time! After that Oban and I went to finish up the VHS stuff that we had done yesterday- this included plugging the wires that we had just run into their corresponding radios. All that was left was to attach the GPS to the radio, which is necessary for a distress signal, it will send a signal to all those within the field of view that can receive a distress signal along with the coordinates. 

April 19, 2023

Today I worked mostly on UPS testing. This was a bit more complicated than I had initially anticipated, yet the directions seem simple: 

Locate the UPS

Identify any electronics that are plugged into the UPS (each of these need to be shut down and unplugged prior to testing the UPS.

Determine the Power output limit (in Watts)

Consider known electronics with power inputs good for the test and plug in.

Unplug the UPS

Time how long the battery lasts.

The first UPS that I worked on had quite a few difficulties. There were 4 things plugged into this UPS. Interestingly the first one was a desk light, which I suppose is important in emergencies so it makes sense. The other things are, 2 navigation monitors, and a “Man Overboard” alarm system. This seems simple enough except one of the wires was not labeled and so I had to trace it back to where it was, which required going up through the ceiling panels and finding where it originated. 

Before I was finished locating the other wire, the scientists came on board today to begin “mobbing” (mobilizing) all their supplies and equipment. I helped them install a Transducer to send out a signal to communicate with an acoustic release- this is what releases the mooring during recovery. Installing it involved just a few bolts and some more wire feeding and management (hurray) but it was in a part of the ship I had not seen yet! It’s on the first deck behind a door that looks like it is sealed shut and hadn’t been opened in many years. This opens to a small cavity about 2ft x 2ft square that extends down to the hull of the ship. This cavity is generally called a “moon pool” but on this ship is called the straza tower. Here you can see a picture of the transducer that we installed. 

After we were done with that, I went back to the UPS’s and managed to finish 3 of them. You can see the chaos required to figure out sources for each of the UPS. Luckily most of these wires were labeled which made it relatively easy.  

April 20, 2023

This morning, Oban and I worked on assembling the wire after it had been unplugged from the CTD for the winch tests. Managing wires is especially important on the CTD because of the conditions it is sent to. Normal wire management is to keep everything neat and organized, but managing wires on the CTD is to minimize drag and force being applied onto the wire. The way to do this is by zip-tying the wire throughout the CTD and along the metal frame. 

Unfortunately later it was determined that we needed to terminate the wire so all we had done was immediately undone. However it was really cool to see a wire termination as there are a LOT of steps to make sure everything goes properly. We took off about 30 ft of wire. Wire termination consists of attaching the winch wire to a port that connects to the CTD and also keeping everything structurally sound. Since the wire is directly attached to the CTD, it is imperative that the load is taken off the bottom part of wire where it attaches in order to keep a good connection. Once we terminated the wire we did a quick weight test and connection test to make sure we can still communicate with the CTD and that the wire can hold it too.

During these tests, the A-frame was noted to have been a bit strained and warped by the previous weight testing and so the hydraulics will need to be checked the next time there’s heavy maintenance on the ship. 

Later I went and updated many of the computers aboard the ship. This entailed doing a windows update, a chrome update, and an antivirus update. Simple enough it was just time consuming. 

April 21, 2023

Deployment day! Today we are deploying on the “conte” cruise. This cruise we will be recovering and re-deploying a 4,500 METER LONG MOORING!! :O 

We had a meeting discussing the recovery and deployment of the mooring and apparently what we do is grab the bottom end first, and then pull in all the way to the top. Now this sounds easier than it apparently is- with the process generally taking approximately 4-5 hours with a possibility of another 6 hours if anything goes wrong. (Fingers crossed that it goes smoothly.) 

Today consisted mostly of transportation and a few tests of the conte machinery. 

First we tested their acoustic releases by sending them down to 1,500 meters and seeing if the transducer would communicate with them properly. Everything worked well! It was really cool to hear these machines communicating with each other. Essentially there are a series of patterns and codes that are sent at specific frequencies to the acoustic releases and once these patterns are recieved you can listen for the response- in this case it was 4 high pitched quickly repeated “chirps.” In order to do this test we obviously needed to turn off our acoustic echo sounder- which runs at 12 MHz, similar to the communicator. After the test was concluded, we prepared for a short pump deployment.

These are going to be very similar to the pump deployments of the bats cruises where they pump water through and collect the material in a filter. 

We will be doing a few pump deployments this evening and then first thing in the morning (even before breakfast) we will begin the recovery. 

Unfortunately the cruise was postponed so we’re heading back to port for the time being.

April 22, 2023

Today we made it back to the dock and since we got back towards the afternoon we got the rest of the day off as it was the weekend. Rory mentioned that the cruises might be postponed for a week or so, and if I can get my return flight postponed as well I might be able to join them still. Working out the semantics- fingers crossed!

April 23, 2023

Today was a very quiet day, it was Sunday so we had the day off and I took the opportunity to catch up on emails and rest.

We had a nice little barbeque for dinner. It was very fun and much needed. Towards dusk I pulled out the guitar and we all sang and played songs.

April 24, 2023

Today we’re working on demobilizing and each of the techs are working on a cyber-security certification. 

I hope they let me extend my stay so I can get on at least one more cruise. 

 

Introduction

Hello,

It is a great honor to be selected for this internship opportunity. I am a full-time student at Northwestern Michigan College pursuing a Bachelor’s Degree in Marine technology and will be graduating this Summer with an Associate Degree in Applied Sciences with a focus on Marine Technology. The ROV and robotics side of marine technology are my favorite subjects but I’m also very interested in sonar and bathymetry. I have always had a great appreciation for the lakes and oceans. I enjoy learning about marine habitats and marine biology. To say that I am excited to get out on the R/V Hugh R. Sharpe is an understatement, I can barely contain my excitement.

 

Achievements

  • • Dean’s List Award from Fall 2021- Fall 2022
  • • 4.0 GPA in Marine Technology courses

Activities

  • Working on cars, tractors, and motors
  • Enjoying/learning about nature and animals
  • Creating/repairing circuits and electronics 
  • President of the NMC Rotaract Club 2021(sub-group of Rotary International)
  • Rotary International Exchange Student – Germany

Week 2: BATS Cruise and CTD’s

April 10, 2023

Today was a windy and rainy day, but luckily most of our tasks were inside the ship, so wet gear was not required.

First I helped Oban install a new PC for an existing CCTV camera that points towards the CTD winch. It involved wiring, updates, program installation, and a little bit of hardware to mount the PC and keep it from moving during deployment. 

Then I helped clean a net deployment latch that had gotten covered in glue and sponge for some reason, and thus didn’t function well.

Then Lydia had me go down to the lower deck to open up the Pinger to get diameters of the O-rings and check the battery sizes, so that the techs can order and replace them. It was heavy and hot down there, and I was down there for about an hour. It took much longer than anticipated because measuring the O-rings was not easy. Eventually I took a rough estimate, went back to the tech lab to look for the possible dimensions, and then went back down to see which ones matched closest. 

April 11, 2023

This morning Rory (Mentor) showed me how to check and replace batteries for the UPS’s on board. UPS’s (Uninterrupted Power Supply) are essentially a temporary backup power supply for when the main generators malfunction and the backup generators need time to turn on. Machinery and sensors are plugged into these so that when there is a power failure, the UPS jumps to battery usage and keeps the device powered up long enough for the generators to kick in. There are many already installed aboard the R/V AE, however there are a few old unused ones that need testing and battery replacement. You can see an opened one below:

Rory gave me 3 of them to work on as a side project for when the main techs don’t need any additional help. Once I loaded them on board, I had a side project with Oban.

I helped him install a PA system from the tech lab to the lab on the bow. This required wire management with zip ties and terminators with crimps instead of soldering. We also used an interesting insulation material that is gooey and sticky for internal wire insulation that we then sheathed with stretch tape. We initially were going to use heat shrink but it didn’t fit after the insulation was added. 

Once the PA system (a horn speaker) was attached to the bow lab, we had to feed the wire back to the tech lab. This required going from the outside to the inside which meant going through a watertight port. These ports need to basically have removable and accessible wire ports but also remain watertight when not in use. Unfortunately the removal and addition of the wires is not easy. It requires a lot of finagling. Plus, if the rubber material (seen in image) is at all decomposed or corroded, it makes it stickier and more difficult to remove. As can be seen are the little blue and black “rings” around each of the wires. 

Each of the rings can be either added or removed to accommodate different wire sizes. These rings are composed of 2 varying sized “rectangles” that are wrapped around the wire to create hollow cylindrical hemispheres. Interestingly, though I’d expect to use small bits of thin glue to keep the rectangular rubber pieces surrounding the wire in place, instead you use lubricant! Also, instead of building the rings around the wire, there’s a hemispherical “pocket” that each of the rectangular ring inserts will sit, and then once enough rubber material is built up, the wire is sandwiched in between and then forced back into the main component. For reference, removing and re-inserting required the use of a punch and chisel, as well as a big rubber mallet, and lots of patience and force. By the end of the whole debacle Oban and I were both red in the face and sweaty, no thanks to the perfect yet warm and humid Bermuda weather.

Throughout the day I also got lots of practice with finding where everything is in toolboxes which I’m sure will be very helpful. 

Towards the end of the day I took the 2 UPS with newly replaced batteries (the third is not turning on so requires further investigation) and set them on an overnight charge to test later.

April 12, 2023

Today we leave for a cruise! We will be departing at around 1300. Apparently we would have gone earlier but can only leave when the tides permit, so before then we started off with a safety briefing and fire drill. Apparently I have some responsibilities in regards to the fire- taking care of scientists and whatnot. I’m not sure who’s idea that was (just kidding.)

Oban and I then tested the audio system that we installed yesterday. 

I put on seasickness patch just in case.

On cruises techs have 12 Hour shifts instead of 8 hour shifts. I’m a bit nervous, hopefully I’ll be able to sleep and rest up plenty to have enough energy to be helpful. The tech’s schedule is 3am – 3pm. My schedule is set to overlap each of theirs by a few hours and is tentatively 9am-9pm, unless there is a significantly interesting operation on deck that the techs want me to be a part of lying outside of the 9 to 9 window.

I need to get everyone’s WhattsApp so I can talk to them later. I hope they add me.

Set off on the cruise and so far so good! I was feeling a bit queasy during our initial transit but since I used the seasickness patch it wasn’t too bad. I was also feeling exhausted, so after I took a quick nap, everything was fine! I think I can officially say that I’ve got my sea legs. 

We did 2 CTD casts during my shift today. I got to watch both of the deployments, Lydia is an old hat at this. The first cast was a shallow water cast at 500m. For the second cast at around 3500 m, we removed the PAR (Photosynthetically Active Radiation) sensor because it is “only” pressure rated to 2000m. This sensor is used to record the light penetration at depth, and of course is only really useful for the first hundred meters or so. We then replaced it with a sensor that can determine how many rotations the CTD experiences on the way down and back. Lydia invented this device, and mentioned that it uses an internal compass. I think that it operates assuming that it is always positioned upright? The MT’s are unsure if the rotation of the CTD affects the data, but Lydia mentioned that this sensor is just to begin observing to see if it does affect it at all. I assume that the rotation of the CTD does not affect the integrity of the data too much, but likely does affect the load bearing that the wire holding the CTD can handle. 

We can still see the shore of Bermuda which is nice because it gives orientation. I was kind of hoping to go out so far as to not see it anymore, so as to feel entirely isolated and get the full “at sea” experience.

April 13, 2023

First night wasn’t entirely restful, but I did get some sleep. I kept falling asleep and then waking up again. I think both rocking and the goings on in the ship kept me awake with the occasional door slams and “bumps” in the night. Tonight I’ll try ear plugs.

The first thing I did was observe the PITTS deployment which was quite fascinating to see. There are a bunch of tubes oriented vertically with the tops open all held in a rack, 5 tubes per rack. All along a line these racks are placed in with a weight at the bottom of the line. There are many lines severed and strung together with proper connections, each break in the line is where the basket of tubes is placed. At the top there are large buoy’s that keep the line oriented vertically within the water column. The goal for each of the tubes is to remain suspended at different depths of the water column, and collect “marine snow” during the entirety of the deployment. At the surface of the water there is a floating buoy with a large pole extending up as pictured. This is satellite communication so that we can go and find it again.

After that we did another CTD cast to 1200m, and upon retrieval we could see that the containers 16 and 24 did not fire again. Apparently Lydia had isolated the problem last night and it was determined that the mechanism that triggers the magnet that closes the cylinder is no longer water tight. There are ways that this can be temporarily fixed, but it seems that that method had already been used, therefore Oban decided that we should replace the mechanism altogether. There is a website that is used to keep track of all the tools and equipment on board, and in what state they are in. Checking this we could see that there is another mechanism available for use in the lower deck MT storage compartment. Oban and I went and grabbed it and began working on replacing the one on the CTD with the one that was in storage. This required moving some of the cylinders and wrenching bolts in awkward positions, you can see the removed cylinders in the picture below.

There was a little confusion on how to remove the current mechanism but luckily we were able to remove and replace it without difficulty. All this occurred while they were also doing plankton tows, and so had to stop what we were doing every 20 minutes or so. 

Now all that is left is to see if we replaced it correctly, and the only way to do that is to wait for the recovery and look at it in person.

At around 900 ascending CTD, the scientist on duty Alfonso and I noticed that the secondary salinity sensor appeared to be misreporting data. The difference between the primary and secondary was huge. After that the oxygen sensor began to malfunction as well. Oban mentioned that likely the cap came off while ascending, and since the salinity and oxygen sensors are on the same casing, it makes sense that they are both misreporting data. Interestingly though, the secondary temperature sensor seems to still be functioning fine, which is strange because it is also with the oxygen and salinity sensors. Here you can see how different the sensors were reading data. On the left is the good sensors, and in the middle is the haywire sensors and the innacuracies represented by all the horizontal yello lines.

 I suppose it’s things like this that are why we have backups of everything. Apparently the fix for this is a simple one, but unfortunately it seems we’ll have to wait until the CTD is recovered to fix it, then plug in the cover again. 

CTD successfully recovered! Unfortunately they don’t know what the problem is with the sensor, so Lydia and I replaced it with one of the backups. This required crawling underneath the CTD and loosening some screws. Here’s a cool image from below.

It appears that all the bottles successfully fired which means Oban and I installed the center mechanism properly. One bottle didn’t close correctly, but that was due to the lid being askew rather than the latches misfiring. 

We then did a C-OPS with Matt, which I still don’t fully understand, but I believe it’s a callibration test for the sattelites, which involves letting a line trail behind the boat until the sensor reads 85m and then pulling it back up and doing it another two times. It’s quite rudamentary in that you just drop the wire in and then all hands on deck grab and hoist the wire back up. Deck hands are basically running back and forth in order to retrieve this wire. I think next time they’re debating trying this with a block on the big A-frame in order to make it easier to pull.

I plan on working on the UPS later this evening, because we have a deep core with the CTD and that takes a long time, so there should be time in between to work on the UPS.

We sent the deep core CTD down and I got to deploy it myself instead of just watching this time!!!! It was super cool. 

I started working on the UPS after the CTD deep cast deployment. However I stopped a minute and a half in because the noise was unbearable and people are sleeping downstairs. I even had first mate Emmy come check to see what the noise is. I tested the grey 290W-360W with two box fans which will take up approximately 200W-210W. A good test will run for about 20 minutes, but having the alarm blast for 20 minutes straight didn’t seem like a good thing at the moment with people sleeping. I may try this again if I can find a plug outside. 

Towards the end of the day I had an hour left and decided to open up the “junk” UPS again to see if I could further isolate the problem. This UPS is from 2011, and something in it doesn’t work. The past few days I’ve been taking it apart and testing it with a multimeter and batteries but it’s quite difficult to reach into, and we’re dealing with 120V AC power which can be quite dangerous. When plugging the UPS in, it doesn’t even turn on and there is no DC voltage coming out of the battery leads. Today I was able to determine that the UPS is indeed getting 120V AC power initially, but somewhere between the AC input to DC converter there seems to be a problem. An hour had passed by and so it’s time to clean up and try again another day.

April 14, 2023

Today started out with an already deployed deep cast where all there is to do is wait for the recovery so for the first part of the day was relatively uneventful. In order to pass the time I decided to test the UPS again. This is the smaller grey one that has a max wattage output of 300W. In order to get an approximate test I used 2 box fans of 100W each to make it a 200W test. Once unplugged the UPS lasted for 15 minutes and 53 seconds. This is decent, but not great. One would hope for at least 20 minutes but then again since this is such a low wattage it likely doesn’t need to keep things on for that long. 

We then did another C-Ops with Matt using a block this time instead of purely by hand. Interestingly I don’t think it helped much more and was quite a bit more of a hassle, but that’s why we tried it is to see if it was worth it. 

Today was my first exposure to a pumps deployment. It’s relatively similar to the PITS sediment trap but this time with pumps. We attached 4 pumps at varying depth to a vertically suspended wire and let them sit for 5 hours. 

Afterwards we did another CTD deployment and while we were waiting I worked on the UPS again. I did a quick test with the black UPS and a 1200W heat gun. This was a mistake however because although the black UPS is much more sophisticated and has a screen with settings, it doesn’t have the wattage output labeled and I had only assumed that it was over 1200W. This was not the case. A quick internet research showed that it’s maximum output was 700W. This proved to be a problem because that meant I had to go looking for different appliances that would ultimately add up to nearly 700W. Phone chargers only use about 20W, iPad chargers use 61W, laptop chargers can use around 1400W. All the things I found used either too little or too much power. Eventually I stumbled upon a “dusting fan” that uses 480W. Pairing this with the two fans would give me a perfect 680W. I also brought out a glue gun to test if the appliances I plug in do indeed use up 680W and if the UPS is rated to 700W output. I did this simply by plugging all the appliances in so the output power needed was 780W, and waited for it to give me an “overload” error, which it did. I then plugged in the duster and fans, unplugged the UPS, and immediately started the timer. Interestingly it only lasted 6 minutes and 41 second, which given the output might be good enough, but I was expecting at least 20 minutes. Because I don’t fully understand the parameters for power and time, I’ll be asking Rory additional questions to see if the UPS works or if it is faulty.  

Lydia is letting me off 3 hours early today so that I can catch an early morning production deployment, I’m not entirely sure what that means. 

April 15, 2023

Woke up at 5 in the morning to do a production deployment. Production is basically the measure of how much C-14 is consumed by the organisms in each of the flasks. These flasks were filled with sea water from the CTD at varying depths, and then injected with a concentration of C-14 and suspended back at those depths. 

Quick shallow cast CTD deployment to 1200. Oban let me do it myself today and said I also might be able to do the recovery. Everything went smoothly.

While we were waiting I went downstairs to help one of the scientists Rebecca with preparing the testing samples by putting filters on nozzles. 

Interestingly, earlier I had assumed that the CTD’s sensor data are what the scientists use for the individual sensor values. However, this is not the case. The scientists will measure the exact data from the water extracted at this depth and then calibrate the generated sensor data to what they measured. 

April 16, 2023

Got up early to observe the PITTS recovery. There were a lot of things going on at once, and everyone had to remain vigilant to make sure they didn’t get caught up in a line. 

It seems that the recovery might have taken a bit longer than expected, because with the following CTD cast, we seem to be behind schedule by at least 15 minutes. I think we have like 6 CTD casts today all back to back to back. A CTD deployment has a series of events that need to happen in concession with the other. First the deployment, you have to be on deck to deploy the CTD. Then you have to run all the way up to the bridge (3 flights of stairs) to begin communication with the CTD. After the scientist has finished the Niskin sampling and the CTD is brought to the surface, you then have to shut down the machine and download the data, then run all the way down to the deck to recover it. This is usually not tiring at all. However, usually there is time between the deployment and recovery, but today they are incredibly short casts. Instead of having one tech run up and down the stairs for deployment and recovery, we will be using walkie talkies to coordinate.

Today is the last day of this BATS cruise. I still need to get everyone’s information. 

Week 1: Flight Delay, CTD, Pumps, and Easter Break

Week 1 Arrival in Bermuda

April 2, 2023

Unfortunately, when I arrived in LA on the 2nd, my flight was canceled and I wouldn’t have been able to make it onto the connecting flight to Bermuda. The only flight that the airline company was able to schedule me on didn’t depart for another 2 days. And so I waited. Luckily the ship wasn’t scheduled to leave for another few days and so though I would miss the safety briefing I should make it for the first cruise.

April 4, 2023

Airplane departs at 11:50pm without any difficulties.

April 5, 2023

I finally managed to arrive and I came right when the staff was having an Easter party. There were games and prizes for different little events. For food there was traditional “Hot cross buns and Fish cakes” which I had never had before, nor would I think to have the combination of a sweet roll made with cinnamon and raisins and inside place a savory fish cake, but it tasted great! Lydia (Marine Technician) showed me to my cabin and said we’d be departing at 9am in the morning. 

April 6, 2023

Luckily even though I missed the safety briefing the day before, they still let me onto the first day-long cruise, and the first mate Emmy gave me a make up safety briefing. This included donning a full immersion suit made of thick neoprene.

This cruise was with BATS, and was only for the day. My goal was to get accustomed to the ship and its operations. There were two scheduled CTD deployments at 3450m and then again at 100m. 

The only problem that arose while on the cruise was the seawater intake pump filter got clogged. It was noticed by Matt, one of the scientists, who saw that the flow rate of sea water had significantly decreased. Oban, one of the marine technicians, knew exactly what the cause was, “the pump is clogged with sargassum seaweed.” When we went to turn off the pump and check the strainer, sure enough there was sargassum seaweed blocking the flow. It’s got small pneumatocysts that hold air. When chunks are broken off from the main organism they float to the surface. This is a problem for valves that intake seawater under the ship because the seaweed is floating at the top and will get sucked up instead. Once the algae was cleared, once the pump was turned back on we could see that the flow was moving smoothly again.

While we were checking the flow rate, Oban had noticed that the fluorescence of one of the sensors was significantly different than the other. Since the day was almost done he wrote it up in the to-do log to check on the next maintenance day. He mentioned that a good way to tell which one is off is to compare the values to the CTD fluorescent values and likely the one that matches is the one that’s accurate.

Once we got back to shore, some of the crew and I went to a local restaurant called “White Horse” where I got a ginger soda. 

When we got back to the ship, Emmy told me where the “soft” blankets are, and that there are a limited number of them so I should grab one while I can!

April 7-9, 2023

Apparently the marine techs have this weekend and Friday off, which leaves me plenty of time to rest up, adjust to the time change, and explore. 

Luckily one of the crew said that I could use his bike, and so I’ve been riding as far as my legs could take me. Rory also lent me some bus tickets for a bus that runs all over the island, though I’ve yet to come close to following the bus schedule.

P.S.

A lot of the people on the R/V AE have accents from all around the world, and I noticed myself inclined to mirror them. I remembered hearing that there’s a phenomenon that after you spend a lot of time with someone with a different accent you’ll pick up a bit of it. A quick internet search found that this is called the chameleon effect, and is a natural occurrence where we unintentionally mirror others in order to bond and feel safe in social interactions. So it stands to reason that I will eventually adapt an English, Australian, Filipino, and a swashbuckling West Country “Long John-Silver” concoction of an accent. I endearingly look forward to it. 

Pre-Departure Introduction

Hiya! 

My name is Brianna Roberts, and I just graduated from Cal Poly SLO with a BS in Ocean Engineering. 

Some of the hobbies I enjoy are playing guitar, Surfing, painting, hiking, and free diving.

I have been passionate about the ocean for as long as I can remember. Solving problems and helping the ocean are what I want to incorporate into my career. I have some experience working on boats for my senior project. We built and deployed a deep sea lander with a video and bait system pressure rated to 1200m.  

I will be leaving for an internship aboard the R/V Atlantic Explorer deployed off of Bermuda assisting professional marine technicians for all the cruises for the duration of the month of April and into some of May 2023. I expect to learn how to deploy the different equipment that is aboard the R/V AE as well as fixing and cleaning various components when needed. I am so excited to immerse myself into the role of a marine technician and make connections along the way. I hope that this will open the door to many opportunities in the future revolving around Ocean Engineering and discovery. 

Thanks to Maria Osiadacz for this incredible opportunity and to the people that have supported me to get here!

Week 8: Final Week aboard the Armstrong!

12/12

Final week of this internship! Despite being done with INSURV there was lots to do around the ship, many of which included cleaning up and reorganizing after the inspection. As the ship is going to be in port until the new year we took off the CTD and put it on the dock, where it will get taken away to have all its sensors calibrated. Most of the sensors need a calibration every year or every other year, and with the calibration log I worked on earlier in this internship it was clear all the sensors onboard needed calibration. 

The engineers are working on a project of their own, rebuilding one of the engines. This doesn’t overlap with the technicians at all, apart from needing to open a hatch on the starboard side deck. The hatch in question happens to be underneath the tracks for the CTD cart. So this meant for us, once we offloaded the CTD we started work on doing all the bolts for the track pieces that cover the hatch. Luckily the whole thing didn’t have to come apart, and we could get away with removing only about half of the track. 

This made for a great opportunity to pull off the gaskets beneath the tracks, they were extremely gross and caked with salt deposits, so one of my tasks of the day was scrubbing these gaskets.

My scrubbing was interrupted in the afternoon however, because of a small operation to bring the ship port-side into the dock. This was done to make life easier for the divers who were diving on the sea chest on the port side. Now, the ship can dock on either side, but they really prefer the starboard side as the decks have been designed with that in mind. This just meant for me, I had a very interesting time running the fiber internet cable from the connection on the starboard side all the way up to the focsle deck and over to the port side. Where there is a will (and enough velcro) there is a way, and soon the internet was restored! The ship will stay docked in this position while the divers complete their work over the next few weeks. 

12/13

Tuesday I finished scrubbing the gaskets for the CTD track, and I also re-labeled them so hopefully whoever has to resemble them has an easier time. After working in the morning on the gaskets, the deck crew was ready to bring on our wire baskets containing all the things we took off for the inspection, and the rest of the technician’s day was devoted to unloading the wire baskets and re-organizing everything in the hold. This proved a much more difficult task than taking everything off the ship, as we put everything back on we really tried to figure out exactly what it was, and if it was a back up that we needed to bring with us at all times. We were able to purge some extraneous equipment, but with the equipment we kept we labeled it obsessively and organized it much better than it had been. Part of being a technician aboard a ship like this, I’m learning, is keeping track of your processes and logging what you do, because you’re not on the ship all the time, the other technicians need to be able to figure out what you did during your time here.

12/14

The weather has gotten much chillier these past few days, but I found a great way of warming up, also an important one, cleaning all the hardware for the CTD track. This track is exposed on the deck to the elements and I believe the technician said it had been taken apart last year, only a year later it is already caked with salt and corrosion, as you would expect. My great task was standing over a sink running very hot water to clean all of the bolts and plates used to secure the track to the deck. This allowed me to stay in the relative warmth of the wet lab over a nice steaming bucket of bolts. Most bolts only needed cleaning with a wire brush, but some plates used to keep the track together needed some extra care with a wire wheel attachment on a drill.

Cleaning these little pieces took up most of my day, until we were informed about a delivery of a new lithium cabinet. This cabinet was deemed necessary by the Shoreside people as we have many tools that use lithium batteries. The battery containment unit is on wheels, but if you’ve been reading this blog you know that this ship rocks quite a bit, so a good part of the cabinets design is that it is intended to be able to put fires out on its own. As I understand it, the battery is placed inside the cabinet where the fire suppression system keeps it at bay. Of course, hopefully we never need to find out!

12/15

Thursday began very windy and rainy which was unfortunate for the new printers that have been delivered to the ship. They were out of their boxes already but wrapped with shrink wrap, so we believe not too much water got in, however these new printers are not the ship board technicians job to install. As I understand it Shoreside support will send people to install the printers, leaving us free to pursue other tasks today.

Emily and I moved on to removing some plumbing from the port side and contaminated sea water pump, which is all the way up in the bow thruster room. The corrosion on the plumbing for this pump was quite severe, and it took both of us to pry the pieces in question off. Once we got the pieces off, we sent them down to the deck crew for needle gunning and painting.

The next task of the day was taking apart the motor for the CTD track, which had suffered the same fate as the track itself (very corroded). An interesting detail about this motor is it appears to have as many as three different types of metal used on it, one of them being aluminum. We did finally get the motor apart from the driving gear, and the pictures will tell you how difficult it was!

12/16

Here we are at last, the final day of this internship. Unfortunately for you readers, it wasn’t the most thrilling of days, finishing up an internship like this has a lot of paperwork involved. Luckily it was a rainy day and no one was working outside anyways.

I want to thank everyone who has been reading this blog, and keeping up with my adventures! This internship has meant so much more to me than I could’ve imagined two months ago.

As I wrap this blog up, I can now say that part of the reason I had so much paperwork to do on Friday was not only the combination of the internship’s paperwork, but also I began the process of new employee paperwork! I feel so lucky and privileged to say that Woods Hole Oceanographic Institution has hired me on as a casual technician for the Armstrong. This will allow me to train with this ship’s systems a whole lot more and I will be joining them on a few cruises in the 2023 schedule. While I won’t be blogging those experiences, this internship has definitely reinforced the importance of noting everything that I’m doing, because the time really does fly!

Week 7: INSURV

12/5 

We began the week with three days left until the INSURV inspection, and everyone was running in high gear! In the morning I added the final coats of paint to the bullseye on the platform and Emily and I started working on fixing the gaskets for the CTD platform track. The track goes over several deck plates and hatches, and the gasket eventually gets displaced as the ship rocks. Putting it back into place just meant undoing the bolts holding the track, and (professionally) shoving the gasket back under. This also gave us an opportunity to work on the track itself, grinding down any corrosion and aligning the track pieces better. This, along with the motor rebuild Emily did last week means the CTD cart has never moved smoother! 

As rain came in for the afternoon, I shadowed Sonia as she updated any out of date workstations, which can be a delicate process for some machines that operate a specific version of Windows or Ubuntu. This is not a quick project so we busied ourselves with other minor projects for the rest of the afternoon while also babysitting the computers.

The weekend had a slight glum, after the cold weather and only short trips around town my car was dead! We went to the front desk of the Smith Laboratories to borrow a work truck to jumper it and the security guard there said “I’ll do you one better” Thanks!

12/6

The rain continued into Tuesday so we all continued inside projects, most of which included continuing computer updates and cleaning, yay! I worked off and on between checking for security updates on computers to cleaning down in the transducer room. The transducer room is vast so some deckies were cleaning down there also. They painted and dusted while I cleaned off all the tops of the transducers and transducer equipment, and also scraped off tons of excess masking tape on pipes. 

The big success of the day was removing the tape from the CTD platform, finally revealing my masterpiece, the bullseye!

This process was challenging for me technically to combine all my skills recreating the pieces and fitting them together, and then artistically painting the bullseye in Rustoleum so that it could be seen from the winch operator’s booth (since that’s who this is for, so the winch operators have something to aim for). Overall I think it came out great, and it gives everyone a laugh when they walk by!

We finished the day at the tech’s weekly meeting in person, where everyone wished us luck on the upcoming inspection. 

12/7

Final day before INSURV! The morning started with meetings for the SSSGs and then frantically finishing up all projects. For me this included a final round of cleaning in the labs and staring hard at all the SSSG spaces, trying to find things that had been missed. The crew worked so hard preparing for this inspection, the ship is looking spotless! 

I fine tuned my little bolt cover for the CTD, as the last one was too small by about 0.5 mm. This proved an exercise in frustration as the 3D printer decided for half my prints to stick, and half of them to unstick part way through. The machine cant be blamed for this (as much as I’d like to) and it just keeps printing as if nothing happened, leaving you with a wonderful ball of filament spaghetti in the end. Eventually I printed enough good ones to attach. 

12/8

Everyone woke early for even more last-minute preparations, but before we knew it, we had almost twenty Navy guys onboard setting up in the mainlab. In the briefing before we set out from the dock the Navy commander gave us a run down of which departments would work with which inspectors. They also explained that this team solely does inspections, moving around the country doing all the Navy ships. The techs were assigned one inspector who specialized in IT and the process began! 

We departed the dock at the 1030 slack tide, with plans to steam down into Vineyard sound for the propulsion tests. The INSURV inspector followed us around as Emily and Sonia explained how the network is set up onboard and answered his questions about the servers and router(s). It was very interesting to hear him compare the Armstrong to other Navy ships, we must seem tiny! The Navy guys were especially impressed with the food, complementing the stewards endlessly. The tech inspection finished quickly after he checked out all the server racks and printers, then we were free to lay low until our next test. 

After lunch the techs gathered back for a CTD cast, which was quite short because we were only in about 25 meters of water. The goal was just to demonstrate the operation of the LARS arm that deployed the CTD, and this was also a test for the termination I did, luckily the CTD operated well and my termination held! (losing the CTD in front of the Navy might have been the subject of my nightmares)

This concluded the inspection for the techs, and we got to relax a bit while the deck crew did more operations on the way back for slack tide at 1545. After buttoning everything up for the night, it was time to get some rest for the last part of the inspection tomorrow!

12/9

The INSURV team was back bright and early, continuing with the rest of the engineering checks at the dock. The techs hung out for any questions that might come up, but the only ones were helping the team connect to the wifi. The team then left before lunch without much fanfare, but during the crew debrief we were told just how well we scored and then the celebrations began. Overall the Navy sounded very impressed with the ship and especially the crew! 

I spent the afternoon fixing the only thing the tech department got dinged on, which was missing screws from the server racks, and easy fix. I then moved onto investigating an ethernet cable that had stopped transmitting, apart from the crusty corrosion on the termination, another bad sign was when I cut the cable and water started dripping out. Sonia helped me to find a replacement cable to run and I re-terminated the end to fit where it needed to. While we aren’t sure how the water got in the cable, the sun was setting and I lost the light to finish the project. 

Weekend plans no longer include a short cruise, as the wave conditions were forecasted to be rough. This just means we have a more relaxed window to set back up after INSURV. Another disappointing note is we wont be installing the new ADCP transducer this week either. While we had the transducer itself onboard, the parts for the elevator needed to lower it through the sea chest are not ready yet, so the project has been tentatively moved to February. I am disappointed of course, this install promised to be a great learning experience involving multiple departments onboard, working together to install a transducer without taking the ship to dry-dock. However I know Emily has other projects we can dive into this coming week! 

This by no means leaves us bereft of projects for this last week! INSURV gave us an opportunity to purge and clean, and this has unearthed several projects to keep me nice and occupied. 

Week 6: Inspections, 3D prints and CTD Terminations!

11/28

    We woke after the Thanksgiving holiday with a full crew again and lots of things to do! The techs first task was to test the .322 cable used for the CTD. This testing involved the use of a Megger instrument to test each wire within the cable for insulation resistance and a few other things.

The insulation resistance (as the name implies) measures how well insulated the wire in question is, and this mainly tells us how damaged each wire is. The techs test the cable before and after cutting it each time for re-termination, and the results compared to each other are how they gauge the health of the cable. A high insulation resistance reading means the cable is performing well, and a low reading (especially compared to a previous reading) means its probably time to re-terminate. 

    The techs re-terminate this highly-used cable about every six months or so, so when our readings were complete and to no one’s surprise, the numbers were a bit low, Sonia handed me the angle grinder and had me cut the cable. 

(The new end, taped up and ready for re-termination later this week!)

    We then all moved onto one of the biggest tasks, removing the hatch from the science hold to empty the space of all the SSSG equipment. The hatch was unbolted and wire baskets were lowered down!

We ended up filling five baskets with secondary and backup equipment! It took most of the afternoon but in the end it was great to get this task done at the beginning of the week while we were very motivated! 

11/29

    The weather prevented some outdoor operations, so we worked on inside projects like securing the cable runs in each lab space and taking down even more unnecessary runs. 

    The biggest excitement of the day was a run to Home Depot! Sonia and I used one of the WHOI trucks available to employees, (since the plywood we needed definitely wouldn’t fit in my car) and drove up to get some 2x4s and sheets of plywood to build a new platform for the CTD cart. Construction on that project will begin tomorrow!

11/30

    I began the long process of cutting all the pieces for the new platform. I use the term long, not because I had trouble cutting all the pieces out, but because all the pieces had to be fitted to their individual spots on the cart frame as I discovered none were interchangeable. Once I had all the pieces cut out I used an orbital sander to fine-tune the pieces and bevel the edges to fit close to the frame’s weld seams. This maybe was not the ‘proper’ tool for the job but with the roughest grit sandpaper I could make sure each piece fit perfectly without hefting a large saw around. 

    During the day most of the crew was occupied for an ABS (American Bureau of Shipping) inspection, the first inspection group to start our battery of inspections in the coming week. To stay out of their way we fitted all the pieces of the cart in and screwed them down, before adding the plywood and ensuring the new platform was stable. Unfortunately we had to take the platform apart for the next step in my process, paint!

12/1

    Today’s inspection was from the Coast Guard, so the techs again tried to stay out of the way by spending the morning securing more cable runs. If this sounds repetitive by now just remember I can only cut so many zip ties in a day before needing to move on to another project! Also you might be shocked at the sheer amount of cabling on a ship! 

    On a lighter note I was given a full tutorial on how to access the 3D printer onboard wirelessly and also spent time today fine-tuning my designs for parts the engineers wanted us to print. These were the outlet covers and end caps, and after a few re-designs I had two functional parts that can now be printed on-demand when they are noticed to be missing. 

    The only part of the inspection the techs were expected to participate in were the drills, these being a fire and an abandon ship drill. As we have practiced before, at the sound of the alarm we gathered our immersion suits (no one needed to put any on this time, thankfully) and life jackets and mustered ourselves in the main lab. A key to mustering for a drill is (in colder months) DRESSING FOR THE WEATHER OUTSIDE. When I got onboard it was stressed heavily in a real emergency at cold temperatures, evacuating in flimsy clothes and then freezing to death anyways was not the goal. The coast guard in a debrief later praised us all for being so prepared. 

    After the drill I embarked on the final step of the new CTD platform, the paint! This is an attempt to keep the platform from degrading with the repeated saltwater it gets on it. I say attempt here because we all know trying to keep saltwater out of places to prevent rot or rust is almost always an exercise in futility. In the spirit of trying to keep the wood from turning green and rotting beneath the CTD the techs told me to try painting it to seal it a bit more. After some research we learned that some types of paint we already had onboard, namely the Rustoleum, could also be used on wood! 

    This led us to conclude that the easiest and most efficient way of getting this platform done was to use that paint. I began by giving the plywood a light sanding with my friend the orbital sander, and going over the boards with a cloth to sweep all the dust away. I then covered both sides of each board with the Rustoleum primer, leaving them to dry for more paint tomorrow!

12/2

    Happy Friday! Thankfully we didn’t have any inspections today so I jumped right in with the first coat of white on the platform boards. I was told to let this dry for longer as the paint interacts with its primer and the interaction could be interesting because it was on wood. 

    Emily and I then moved on to one of the biggest tasks of this internship, learning that all-important skill of CTD cable terminating! We peeled back the layers of the cable, starting with the shielding layers that also act as ground, taking them back about two feet to have enough of the wires to work with. The cable has two layers of steel shielding which also acts as the cable’s ground, so two strands of this were preserved for attaching to the green ground plug. From here was standard wire terminating, stripping the wire, and blending the wire from the cable into the wire to its respective plug.

Emily then got down to showing me how to solder the wires together without burning the casing, then running layers of self-fusing tape, before adding final layers of vinyl electrical tape. This is done for all three wires encased within the CTD cable, then we added the ground connection which didn’t require soldering. All 4 of these new connections were wrapped with even more tape to attempt to keep as much water out as possible. 

    Both techs stressed that terminating this cable is something done often onboard research vessels, and every tech will have their own way of doing it. 

    We finished up the termination and celebrated! Many people were going home for the weekend so the next few days will be focused on indoor projects and organization. 

 

 

Week 5: End of OOI and Happy Thanksgiving!

11/19

Morning operations were successful as the mooring group recovered the last small coastal profile buoy, with its accompanying sensors and anchor. They also recovered an anchor that was left behind from last week. The wind picked up to a constant 30 knots and our destination that day had us steaming into the waves and pounding down for most of the afternoon. This influx of bubbles under the hull is a very big problem to say the least, as it disrupts the ship’s array of transducers. Not only transducers though, the constant supply of sea water being pumped for the main lab supply and to run through some other instruments was heavily disrupted by all the slamming. Emily and I worked to troubleshoot the PCO2 sensor which seemed to have an array of issues stemming from the interruptions in flow. We initially thought we were successful by replacing a drip sensor that had become corroded, but the system kept emergency stopping itself and the drip sensor was not the biggest problem. 

The evening was taken up by a battery of CTD casts, where we would steam (pound) north for half an hour, and then go out on deck and launch the CTD while trying not to get pummeled by waves coming over the side. In between casts I emptied and organized the cabinet in the HIPAP area, which was suffering from poor labeling and the internal lights for the cabinet were low on charge, making it very difficult to find anything. Many (most) things in there were networking pieces of technology I had never seen before, so I did have to bring Sonia in several times for the game of, ‘what is this and do we need to keep it onboard?’ This cleaning also doubled as a purging of equipment in time for the INSURV inspection, where anything superfluous will be removed from the ship. In the end, I was very pleased with the results!

(Also here is the promised CTD bolt cover final print!)

11/20

    The weather remained the same but the CTD casts were done in daylight today, which gave you more light to see the waves crashing onto the deck! 

    The evening brought a break from CTDs, as the EK80 was turned on for a long transect survey. Meanwhile Sonia started me on a coding journey, first showing me some resources to learn the basics, then setting me up with a virtual computer to test out what I was learning. This was lovingly titled “Intern Playground”, and it’s a place for me to get comfortable with a system similar to the ship’s, while also being safe from killing any of the ship’s systems.

11/21

    The weather gave us a break for the ROV operations, but not before giving us another taste of a bumpy night. Everyone was extremely motivated to finish up though, and the first dive of the day brought up the anchor claimed by the crabs last week. 

    The SSSGs had many meetings concerning an upcoming cruise in December, new ideas for upgrading the email system for the WHOI ships, and the upcoming ADCP installation after INSURV. These meetings ended just in time for us to go back into the main lab and watch Chris snag the final stubborn anchor. This one had fired off it’s linepack, but it had snagged somewhere on the way to the surface, so he had extra line to avoid getting tangled in with the ROV. This final anchor meant the last of deck operations, and the ship turned north to head back home. There were a planned group of CTD casts along the way, but the weather had turned against our favor and by the middle of the night, CTD casts were called off.

11/22

    No one got much sleep as the ship rocked and rolled its way back to port. I was personally attacked by all the items on my desk, in my vanity when it swung open and emptied all contents, and my desk chair when they all went flying during various rolls. I did not, however, fall out of my top bunk, which is an accomplishment. 

    No sleep and a bumpy ride makes for a low-spirited crew, but everyone was bolstered by the fact that we accomplished all of the OOI array goals, picking up all of the equipment and doing many CTD casts and surveys along the way. We came into the dock at WHOI around 0900 and quickly the deck and science crew began unloading. 

    As with the last demobilization days, the SSSGs mainly stick to going through end_cruise  work, moving data to the correct places and shutting systems down. This involved the techs all together to figure out what was wrong with the PCO2 sensor. In the end it was a drip sensor that kept stopping the system, but because with all the air in the systems from the ride, the pressure differences caused spontaneous releases of sea water in weak places in the tubing system.  

    The end of the OOI cruise doesn’t mean an end to the work, as now we can fully turn our attention to the INSURV inspection. This meant for these days leading up to the holiday, zip ties were our best friend, as we have to secure all cable runs. This is just one of the many steps for the SSSGs before INSURV, and all other departments on board will be working through the next week and a half painting, cleaning and securing.

11/23

    Our first full day back on shore was a busy one as the demobilization efforts continued. All the moorings and associated equipment are removed, as none of it can stay for the inspection. Speaking of inspections, many different aspects of the ship need to be looked at, including the fume hoods in the lab spaces, and the hull itself, as we had snagged a lobster pot on our bow thruster on the way back. (No there weren’t any lobsters, we asked.) The divers also exercised the bolts on the sea chest plate. You may say this sounds like a lot of exercising for this project, but they take opening holes in the ship very seriously. For our purposes we aren’t opening a gaping hole to be exact, but the outside plate of the sea chest will need to be removed if we are to install a transducer on an elevator and don’t want to hear it go ‘bump’ on first deployment. 

    On the topic of the new ADCP transducer, one of the scientists on the team stopped by in the afternoon, and the techs met with her to discuss the install. For a few days the team had been emailing back and forth about an issue with the cable bend. After discussing many solutions over Zoom, this scientist who visited agreed that the cable bend was not ideal, but likely workable, as the instrument is only planned to be onboard the ship for a year of at-sea testing. For us this means we can continue with the installation plans, as again, we can’t start this project and have it unfinished during INSURV, so it must be started directly after.

11/24

    Happy Thanksgiving! I am fortunate to be spending the holiday weekend at home, and I hope everyone has a great holiday and eats lots of good food!

I did bring a small project home with me, modeling out two more small parts, one to cover a missing outlet (think a protector you have for a baby, but for a hollow outlet strip) and the end cap for those strips of outlets. I will update progress on the parts next week!

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