Week 4 & 5
May 28th
Today I did inventory on the streamer cable modules onboard the vessel and observed data for the rest of the evening.
May 29th
Happy Memorial Day everyone! I woke up to the whole crew on the bridge deck grilling hotdogs and burgers. There was also cornhole and music being played while we all enjoyed our lunch. It was a great moment for everyone. After lunch I assisted Riley with moving winch cables so we could reroute them to the wet lab. After, me and Riley removed old deck units from the mainlab and placed them in the storage room above the lab.
May 30th
Filled out more navigation logs and observation logs and updated certain data sheets.
May 31st
Fairly easy day. I filled out logs and plotted survey lines for lines 46 and 47 on the ORCA planner software.
June 1st
Today I filled out three more logs and plotted 2 more lines. I created the last log for the last survey line which would be completed overnight.
June 2nd
Today I woke up and immediately reported to the streamer deck to join the recovery of the streamer cable. We ended up recovering 12km of streamer cable because we had to deploy 6km more of streamer to set up for the next survey job. My job was to detach the digibirds off the streamer and remove the batteries out of each one before I placed them on the rack. I did this for nine hours and spent the remainder of my shift cleaning the streamer deck. I also ended my day doing inventory on all the digi birds on deck. We are now sailing towards Morehead NC right now.
June 3rd
Woke up to the boat already docked in Morehead, NC so we could unload and load some equipment and switch out some crew personnel. Claire (another mate intern) got onboard and introduced herself to the crew. After Claire, Emma and I explored Morehead, were able to get a scoop of ice cream!
June 4th
Today was supposed to be our first day of coring but we have sailed into five meter seas. Claire and I ran around the boat picking up stuff and strapping down more equipment. THe seas were so rough that Todd (our new mentor) told Claire and I that the conditions were unsafe to work in.
June 5th
All the sediment coring spots were placed off the coast of North Carolina and South Carolina. Today we sailed to the two north coring spots so we could dodge the southward storm. Our first core was a challenge because we were in the middle of the Gulf Stream with a 3.5 knot current. The core was not stable while dropping through the water which led to us missing our exact coring target. Yet both of our cores were successful in collecting sediment. The scientists were fast to extract sediment out of the cores to test for evidence of gas in the sediment. They would also x-ray the cores and scan them for different materials.
June 6th
Today at the start of my shift I found out that the winch had loose cables from the company that we rented the winch from. We had to coil miles of three string wire cable from the wench so we could rewind back in the winch tighter than we found it. This process started at 5 am and didn’t finish until 6:30pm. After the winch was fixed we were able to do our first piston core. While dropping our piston core our bow thruster started malfunctioning which didn’t allow us to keep the boat stationary enough to let the temperature probes that were attached on the core to collect a temperature reading. Temperature probes were placed on the cores to collect temperatures at different depths of the sediment. The sediment in the core was still collected thankfully.
June 7th
We were able to complete four core drops with no sediment collection but temperature readings were able to be collected each time. For four drops we punctured the seafloor for 8 minutes to get a temperature reading. Claire and I had stayed up late to see the last coring operation of the day through but had to stop all deck operations. At 2 am due to high wind and rain the coring team decided it was too dangerous for deck operations to continue.
June 8th
When I reported on to the deck we were in the middle of recovering another core when around 2:30 pm the winch stopped working. The core was hanging 1500 meters in the water with a broken winch. The technicians, engineers and core guys got together and worked all day on figuring out how to fix the winch. Luckily by midnight we were able to get the winch fixed and recover the first core of the day. Sadly all the time spent on the winch led to us missing other coring spots. Due to loss of time and a troublesome winch coring, operations were over. We had started a 36 hour transit to Port Canaveral FL.
June 9th
Today was a transit day so I spent most of my time cleaning the main deck while helping the coring team clean up their equipment as well.
June 10th
We arrived at Port Canaveral but were unable to enter until an available pilot could sail us in. A pilot boat was able to reach us around 4 pm and drop off a port pilot who took command at the bridge and got us in. I was asked to help with lines off the starboard bow of the vessel with the chief mate and bosun. Once we were tied up everyone changed into clean clothes and went into town to celebrate a successful research mission at sea!
June 11th
At port helping with mobilization.
June 12th
Goodbye R/V Marcus G. Langseth!


